This is what
there was to work with; a 25cc WeedEater FeatherLite 2 cycle
with a broken drive shaft. It had been used very little over
a two season period.
Maybe 2 hours of run time on it. As a plus, it is one that happens to
be easy to start, and the drive shaft was broken at the end, making
repair easier.
First
I made some measurements to see how tight the plastic driveshaft guide
can be bent. Looks like radius wrapped around a 1 gallon paint can will
do. (I know... Hardly scientific. I went by how hard
it was to
bend the guide by hand). A tighter bend will keep the prop from
sticking
way out behind the motor. The guide is very stiff to bend, so making
it feed
through a tube with that tight a radius is out of the question. The
plan is the
make a wood lower unit with the bearing bushing glued in place. (Well
this is a prototype after all).
This
what the original looks like. The deep groove in the middle of the
bushing is for the crimp in the original steel tube. The
first
surprise was when I tried to press it into an aluminum 3/4"
tube.
The diameter near the prop is about .050" greater, and the tube split.
I decided to keep it simple and just press a tube part way on.
The
plastic drive guide fits inside snugly to hold it in alignment (below).
With
the flexible shaft installed, the guide was inserted.
(Boy, that
sound simple. Actually it was a fight since it is so stiff)
Glue
was applied to the upper curved 3/4" part and clamped in place. I
wanted the guide to more or less assume a natural shape; more of a
parabola than circle. Clothespins (clothes pegs) were sanded as needed
and used as wedges to manipulate the guide at various places, while
occasionally turning the driveshaft to make sure it was not binding or
had a 'bumpy" feel. Glue was applied to each peg as it was fitted. It
felt smooth, but it still had more resistance than I would have liked.
I
cut 19
1/4" off of the plastic guide, measured to see how far the metal tube
goes into the plastic motor housing (1 5/8") and the distance to the
bottom of the square cable receptacle is (3"). That means the guide can
be flush with the metal tube, and the flexible drive cable can extend 1
3/8" beyond that.
Now
the drive shaft turns very freely. Apparently much of the drag I was
feeling was due to the length of the shaft and the heavy factory
grease. Before the motor is tested I will dribble a bit of 75W 140
weight synthetic gear lube into the top of the plastic guide.
A slot
was cut into the bottom of the case to glue the fin to the bottom.

Next
step is to affix the cut-off original steel shaft into the "gearbox"
with J-B Weld. I wanted to use the aluminum tubing but the
I.D. is
a little too tight.
Then I want to start the engine
and check to see if anything gets warm inside the "gearbox" before I
glue a cover on it.
If
you are following this, you may be curious why the my "gearbox" is a
somewhat massive rectangle. Below is a Mercury outboard lower section
that is typical of outboard and stern drive designs.
Note
the plate above the prop laying in a horizontal plane. It does two
things... Prevents some of the water from gushing upward as the prop
spins thus wasting energy, and helps prevent air from being sucked
downward by water turbulence, thus making cavitation less
likely. I hope to incorporate this scheme into my conversion as I
may need every advantage. It will be of plywood, as will the fin on the
bottom. I believe the hydrodynamic bulge just above the shaft is
intended to aid in directing water flow. It may be superfluous on a
tiny homemade motor.
7 July 07
The
flexible shaft was shortened and the end made square by careful
hammering in the bench vise. I may clean it well and attempt to
impregnate it with glue or J-B Weld later.
The motor
was again
attached to the shaft, a small quantity of gas-oil mix added and it
started on the third pull after sitting two years.
The
bronze
bushing got very slightly warm to the touch, but about what I expected.
I could swear it is much quieter and a bit slower at top speed than it
was, but that may be because I am used to the newer model.
I
checked the rotation of the motor, made heavy pencil lines on the edge
of the prop blank to remind me which way it rotated and started to
shape the 10°. I checked it again to proper rotation. Made
the
blades with an airfoil shape mostly by eye, but all the while checking
with a dial caliper to make each blade match as much as possible.
When shaped and sanded to my
satisfaction, it was dipped in amber shellac (since I was out of
varnish), and allowed to dry.
I
filled a sturdy old plastic barrel 2/3
full of water, fired up the motor and lowered it into the barrel.
As it entered the water, it slowed quite a bit so I added
throttle as it went. When it was even with the splash plate
it
took about 1/2 throttle. It wanted more throttle as
I continued to
lower it. By levering the shaft against the side of the barrel I could
detect far
more thrust than I had hoped for at about 2/3 throttle!
Increasing
the gas beyond 2/3 throttle made it slow a bit. No idea why.
Anything beyond 3/4
throttle is a waste of fuel. However, since this was in a barrel, a
test on something that was able to move (boat) would be quite different.
I
was holding it by hand in the barrel so the exhaust was near my ear. It
was not nearly as objectionable as it was as a weed cutter.
11 July 07The
transom bracket for an old trolling motor has been repaired. (left over
from one of my less fortunate eBay purchases).
Made
a sleeve to hold the motor shaft in the transom bracket. That turned
out to be very easy. The bicycle gearshift for the throttle
is a
bit of a puzzle as to what is the best way to approach it. Cables are
made one piece today as an assembly, so something will have to be cut
on either the new cable or the old, and a new cable end fabricated.
Also
got fittings to make an exhaust that goes into the water.
12 July 07
This
is the original. A short section or 1/16" O.D. brass tubing such as
found in hobby shops and some hardware stores was placed over the new
(slightly larger diameter) cable that came with the bicycle gearshift
lever and bent to this shape
AFTER
the cable sleeve, and fitting that enters the WeedEater housing was
slipped on.

The
tiller is the end of a discarded carbon fiber fishing rod I found at
the dump. Height
adjustment and swivel for the motor is via a piece of PVC pipe that
matches the inside of the transom bracket. I found it necessary to glue
the 1/2" hardwood strip to the PVC column because
vibration made the motor slide slowly downward when run.

Another note
on the exhaust noise. In the shop with no load on the engine and full
throttle it is objectionable.
As shown it weighs 9.0
pounds (4.08 kilo) So far the investment was $7.50 for the
gear shift lever.
13 July 07
Original
muffler (left). Note the heavy springs holding it on, and the tiny
half-circle
exhaust exit hole. When the plastic rear housing is removed the
crankcase innards are exposed! Newer models have only 2
screws.
Take care to prevent dirt from getting in while you work on a Weed
Eater.

The
copper elbow has a coupling inside it to fit inside the motor's exhaust
port. The edges of the coupling were beveled with a file so that it
will work its way in as it is used, to help seal it. The gear
clamp is wired to the rear spring. Oddly, the two factory springs are
not in a line with the port. The finished tube will hold it
in
alignment, so all that is required is one
spring to hold the elbow against the
port.
Note
the elbow is facing the wrong way in the photo.

A
45° coupling moves the tube to the rear; so that
the the exhaust will clear the transom and transom bracket.
Holes
were drilled, and a single stainless
steel sheet metal screw holds each connection in place.
Above leftThe
lower bracket is aluminum angle, slotted on the crease and bent
slightly to match the copper tube. A stainless steel gear
clamp hold the tube to
the bracket. I made sure the elbow in the port was aligned as I
tightened the clamp. Later, I found it is for the most part self
aligning.
Above
rightAnother
45°, but this time a male/female connector. The small end was annealed
with a propane
torch so it could be squashed to this shape to make the exhaust nozzle
(upper center).
In the shop it is very noisy out
of the water.
The idle is much higher, likely because there is less exhaust
restriction now. It sounds more powerful, revs up
faster,
and starts easier.
Barrel
test 2The
motor is not nearly as loud outside, and a rather pleasant puttering
sound in the water. I can barely pull the shaft away from the side of
the barrel with three fingers, so I am expecting considerable
thrust on the lake next week.
Micro lakeWith
the water level with the
horizontal splash plate, the motor idles nicely (factory setting),
because the exhaust is much less restricted now. Full throttle is
not the screaming you are accustom to when used as a weed cutter. Those
inside the house said they thought it was someone coming up the
driveway from the sound it made.
25 July 07
Experimenting with the height
at 1/3 throttle.It
was a beautiful morning on the lake with about a 10 mph breeze and 75
degrees. The motor started as easily as before and I had to raise it a
little in the water to get the splash plate about an inch under the
surface before it idled nicely.
As I expected, the
noise was
much less than in the barrel; just a gentle purr. About half throttle
seemed the best for smoothness and quiet. Those standing on shore also
said it was just a purring sound.
A wood chip took
roughly 2.5 seconds to go from bow to stern, 2.2 miles an hour, (3.5
kilometers/hour, 1.9 knots) going into the wind. At full
throttle
it churned quite a bit of water behind the boat and there was much
better speed. I did not time it at full throttle. Fuel
consumption was too little to really measure. A longer test may tell
me more.
I am not certain of it, but it
felt like a prop
with slightly thinner blades would work better. I will try to find one
with the 10 degree pitch that can be cut down, or make a second prop of
my own design.
4 August
07 Use this
instead of the wood prop. It only took one evening and works far better.Ordered
a piece of aluminum that will be appropriate for a
home-made prop.
Flipped the PVC tube end-for-end that fits into the transom
mount, then removed about 3/4" from the wood strip that the height
screw bites into. That will allow me to raise the motor just a little
more for the
Flapdoodle.
If I want to try the motor on a boat with a higher transom, all that is
required is to flip the tube back the way it was.
DIY
Prop almost finished
Click image to follow link
I
have acquired an ST-90, 30cc Weed Eater trimmer that needs carburetor
work. It looks well used, but starts easily. This is the type with a
solid shaft, but the motor rotates in the opposite direction from most
small props. I happen to have a prop that should do that goes to a 20
pound thrust Sears trolling motor. If I decide to convert it, it will
probably be the "mud motor" type outboard. The other option would be to
shorten
the shaft and make it more like my FL-25 motor. It has the same lower
part as
this
commercially made small outboard for $450. Note that they are careful
not to show a side view that would reveal its weed cutter
parentage.
8 August 07I
tested the new home made prop in the barrel. Very impressive. The
vibration at idle is gone and it accelerates smoothly to any throttle
setting. The thrust is
far
greater. I have trouble pulling the
lower part away from the side of the barrel. At full throttle it now
bends the
heavy rim of the barrel and pushes water high up the opposite side.
A very nice, quiet little 9 pound motor for very
little investment.
12 August
07 Weed Eater fuel consumptionI
acquired a syringe that is calibrated in 5th of a milliliter. The plan
is to top off the tank, run it for a known period of time, refill it
with the syringe, then calculate the hours per gallon fuel consumption
at several different throttle positions.
Ambient
temperature 92°F
Idle speed = 26.6 hours/US gallon
of fuel
Full throttle= 10.8 hours/US gallon of fuel
However,
the motor shut down after 4.5 minutes at full throttle. I believe the
carburetor gets hot, because I can see bubbles in the fuel line. On a
cool day there may not be a problem, but I really do not see much
advantage to full throttle over cruising at about 1/3 throttle where
the efficiency seems to be best and it is the smoothest running.
AfterthoughtsAn
easier way to make the cable end might be to use keystock
(square
steel) inside a brass or stainless tube all held with J-B Weld.
The hard part is getting the cable clean. Clean everything
with
acetone or lacquer thinner. Rough the cable with a grinding wheel. The
plastic cable guide would have to be drilled to accept the larger brass
end.
Do
not attempt to remove the grease with a propane torch. It makes the end
blossom like a flower.
The
laminated plywood clamp for the tiller was remade in favor of a heavier
design.
I
have also learned I need some sort of bearing on top of the PVC tube so
that the tube does not eat into the wood tiller clamp. Probably will
use a polypropylene disc.
Carburetor
MixtureAn e-mail to me by Sean Miller pointed
this out:
"Just
a note that when you open up a 2 cycles exhaust you really should
richen up the carb. not only to take advantage of power gains but to
keep it from seizing (too lean) especially newer emission engines that
are already real lean as it is. to do it might be tricky on the carb
though probably a pulse jet carb. might have a screw(most likely
not) or may need shimming/bending parts."I
am not certain that I have "opened up" the exhaust, since it is now
under water. 2 cycle engines need a little back pressure to work
properly. Below is information that can indicate to you if you are
running too rich, or too lean...
http://en.wikibooks.org/wiki/Reading_spark_plugs_for_racingA
better view of what colors can be encountered here:
http://www.nh-scooters.com/article/articleview/55/1/2/Another
precaution:
The bronze bearing was not designed for thrust; but for side
loads when cutting brush. It would be wise to repack it with marine
grease before each use to help keep water out and prevent the bearing
surface from galling. It probably would not hurt to dribble a
few
drops of heavy gear lube down the flexible shaft to help protect it
also.
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